Final Report B737 (N278EA) RE at New York La Guardia USA, 27 Oct 2016
Final Report B737 (N278EA) RE at New York La Guardia USA, 27 Oct 2016
On 27 October 2016, a Boeing 737-700 crew made a late touchdown on the runway at La Guardia and did not then stop before reaching the end of the runway and entered - and exited the side of - the EMAS before stopping. The Investigation concluded that the overrun was the consequence of a failure to go around when this was clearly necessary after a mishandled touchdown and that the Captain's lack of command authority and a lack of appropriate crew training provided by the Operator to support flight crew decision making had contributed to the failure to go around.







