Investigation Report BFU EX010-11: B773 (9V-SWQ) Munich Germany 3 Nov 2011
Investigation Report BFU EX010-11: B773 (9V-SWQ) Munich Germany 3 Nov 2011
On 3 November 2011, a Boeing 777-300ER crew lost directional control of their aircraft soon after touchdown and after veering off one side of runway 08R, it then crossed to the other side of it before stopping. The Investigation found that during the final stages of an intended autoland in CAT 1 conditions, an ILS LLZ signal disturbance caused by a departing aircraft had led a flight path deviation just before touchdown and, after delaying a pre-briefed automatic go-around until this was inhibited by main gear runway contact, the crew failed to either set thrust manually or disconnect the autopilot.







